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BRITISH COLUMBIA INSTITUTE OF POWER ENGINEERS INFORMATION NEWS #2—NOVEMBER 2003
by David Goodwin



Report on my Attendance at the Fall 2003 Meeting of the Black Liquor Recovery Boiler Advisory Committee, BLRBAC, Western Canada

BLRBAC is a “Trade Association” that exists for the purpose of generating safety procedures and guidelines that govern the operation of Black Liquor Recovery Boilers.

This organization was formed in 1963 by several groups of concerned professionals that had become alarmed by the number of Black Liquor Recovery Boiler explosions that had resulted in many injuries and death to personnel operating these boilers. These groups consisted of Insurance Companies, Boiler Manufacturers, and Paper Company professionals that were involved in operating, insuring, or manufacturing Black Liquor Recovery Boilers.

The Fall 2003 Western Canada BLRBAC was held November 5—6 at the Crown Plaza Hotel Georgia, Vancouver, with representatives of 19 of the 22 Western Canada Kraft Mills from Manitoba, Alberta, and British Columbia. This provided means of communication from mills with common interest in various aspects of operation.

The conference commenced on Tuesday evening of the 4th with a “meet and greet”. Another social event was on the evening of the 5th. The social events gave an opportunity to speak to vendors, guests, and associates in a casual non-structured atmosphere. On Wednesday the 5th there was a closed session business meeting for BLRBAC members and boilermakers with the main focus on incident reports. Also on the agenda were reports from Eastern BLRBAC, Atlanta BLRBAC, PAPTAC, and other steering committees. Incident Reports

1. ABB Recovery Boiler: rated at 3.4 MM lbs/day, 363,000 lbs/hr steam, 900 psi, 750 deg. F. There was a 1/2 inch transverse crack on the crown of a floor tube adjacent to the side wall in the right rear corner of the furnace. On September 9 at 01:25 it was reported by the Recovery Boiler Fireman that there was a wave motion in the smelt at the spouts. It later disappeared. Then it was discovered that the smelt had burned through the right side wind box and had flowed to the basement burning wiring to the dissolving tank agitator. Later, irregular combustion was noticed in front of the windbox. There was a small smelt pool with erratic waves occurring frequently.

The boiler was taken off liquor and put on gas and inspected again, the erratic waves continued and the boiler was ESP (Emergency Shutdown Procedure) on September 10 at 03:20. The crack appeared to have been caused by a chipping hammer that was used to remove the char bed 2 years earlier. The recommendation: Use high pressure water for char bed removal and restrict the use of chipping hammers. Outage was 56 hours.

2. ABB Recovery Boiler: rated at 4.0 MM lbs/day, 587,000 lbs/hr, 800 psi, and 750 deg. F. Rear economizer tube 17, row 3, had a 1/16 inch hole at the butt weld, 24 inches above the bottom header. At 19:00, May 26, the Recovery Boiler Assistant, during his routine walkdown, observed water in the ash hopper and ESP was initiated. The weld had been done during a regular shutdown. The back part was done by mirror, was x-rayed, and accepted. Notes: The insurance companies require that a walkdown with the soot blowers off be completed at least once per shift. Note: The low solids alarm is at 66% and firing stops at 64% solids content.

3. B&W Recovery Boiler: rated at 2.8 MM/day, 350,000 lbs/hr, 750 psi. On September 17 the boiler was off liquor for about 6 hours when steam and water was noticed leaking from the casing. The boiler Steam Lines 9 was shutdown, depressurized, and a visual inspection made. Leaks were located in the last pass of super-heaters on top of the bull nose. A 1/4 inch pin hole washed out two adjacent tubes causing a 1/8 inch pinhole in each. The initial cause was a cracked tube at a weld termination. This location is not readily accessible during inspections due to a baffle plate. In future inspections the baffle plate will be removed for inspection purposes. Noteworthy is that the mass balance leak detection showed a leak was present 4 weeks before the incident but credibility was not given to the instrument. The outage time was 83 hours.

4. B&W Recovery Boiler: rated at 3.78 MM/day, 563, 200 lbs/hr, 1,125 psi, and 815 deg. F. On October 22 the unit was coming off liquor with the bed burned down when a Field Operator found a leak in the economizer. An inspection during depressurizing resulted in discovery of a second leak, located in the screen tube. The bottom header handhole was leaking into primary hopper. A stress crack in the handhole was ground out and welded. The screen tube had a 1 inch circumferential crack in the butt weld just above the nose arch. The crack was ground out and welded. A hydrostatic test found another screen tube leaking at a membrane termination. It was repaired and the second hydrostatic test discovered another leak in the same tube. It too was repaired. Outage time was 73 hours.

Eastern Canada BLRBAC

  • There were two incidents reported.
  • New Brunswick requires a 4 minute confined space rescue to be in place.
  • One mill has the Shift Supervisor looking after the fibre line.
  • Precipitator dampers must be locked in a secure closed position, both inlet and outlet, for confined space entry in Ontario.

    Atlanta BLRBAC

  • Smelt explosion in a recovery boiler from a water wash, 32 hours after being off liquor.
  • Methods of heat measurement of the bed was discussed.
  • Insurance company asking for alternate ESP in the event the ESP push-buttons do not work.
  • The trend for incidents has been decreasing over the years but now there is a sudden rise, perhaps related to the longer run times between majors.

    PAPTAC

  • There were 3 near misses with oil strainer gasket blowouts.
  • Boiler oil gun gaskets blew out and caused a fire that was extinguished quickly. One reported using superheated steam for atomization.
  • One mill had a tube leak caused by circulation restricted by a welding can lid stuck in the tube. Suggested is a count of all items taken into the drum during maintenance to ensure everything comes back out.
  • Burning 2—5 % sludge with BFB boilers in Ontario.
  • One recovery boiler had a bottom rebuilt.

    Round Table Discussion

  • Out of 4 incidents, leak detection detected 2 and confirmed 1.
  • Loss of cooling water to spouts. Operator put cooling water back on. This could have been a very serious situation that has caused explosions in other mills. The boiler was later shutdown and the spouts replaced.
  • Steam plant Superintendents are coming under increasing pressure to extend maintenance shut-downs to 18—24 months.
  • There are 7 mills or pulp companies in France that are running for two years without a shutdown for maintenance or inspections. They have formed their own insurance company, similar to an insurance co-operative.
  • One company is having initial success with fireside additives. Normally they had to shutdown after 3 months of operation. They are able to go as long as 6 months. The load on the precipitator is down and smoke density dropped from 120 ppm to 60 ppm

    Boiler Manufacturers’ Short Presentations

  • Presentation on electric port rodders improve performance and reliability. They are being used by 2 companies.
  • Gas igniters are like the ones being used by us here in BC on our Power Boilers.
  • New materials for BL spray nozzles.
  • Chromize tubes/composite tubes.
  • Chromize dry spouts. About 70% left after 1 year compared to 35% on wet spouts.
  • It is possible to operate up to 3 years with skilled refractory applicators. Comparative costs are $14K to $7K each.
  • Scrubber performance and upgrades.
  • Air improvements at Thunder Bay from two levels to three improved the running time from 2—14 months with one company.

    Day 2—Technical Session

    Combustion Analysis Around Primary Air Ports. Presenter: Keith Rivers of Aker Kvaerne

    Large Recovery Boiler in China is designed for 13 MM lbs/day with capability of 15 MM lbs/day. Five levels of air input with unique steam membrane panels, one stack, with the dissolving tank flume going back into the RB. Intelligent soot blowers that operate in the areas that are needed — no pre-program sequence.

    Recovery Boiler Air System Presenter: Ralf Holm of Andritz
    Covered vertical air systems.

    Environmental Improvements Presenter: Randy Reeves of Alstrom
    A lot of money has been invested in Electro Static Precipitator improvements with marginal returns over the years. In many mills improvement is required to precips due to their “bottle-necking” the system. The dust pH needs to be tracked. Precip performance tests can be done, inspection recommended before cleaning so that appearance can be checked, corona quenching, mechanical deficiencies, alignment of plates, and tramp air were typical topics. Randy also spoke about particulate size resistively, adhesive characteristic differences between front end and back end. New Epic control has shown improvements.

    Multipeak electrode in the first bank makes significant difference. Different types of rappers may need upgrading.

    Use of Automated Pulse Spray Gas Metal Arc Welding (PSGMAW)
    Presenter: John Grimes of GE Welding Specialty Services

    The GE Company can specify welding electrodes with specific alloys that will best match the boiler. The machines can do 18—20 square feet per shift or 1—1.5 square feet per hour. Unlike with metal spray, the area does not have to be evacuated when using PSG MAW for restoration of boiler waterwall tubes. The weld can be done from 80th thickness and restored to 170th thickness. Maybe it is an alternative answer to a bottom replacement..

    Two Wall Primary Air Systems Presenter: Colin MacCallum of BIAS
    The same amount of air is used but a larger up-flow of gas gives improved retention time, higher bed temperature, reduced emissions, can cut back excess air requirements, cleaner precipitators, and improved reduction efficiency. This system is being used in Western Mills with success.

    David Goodwin



    First published in January/February 2004 Steamlines.



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